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Cequence Energy Ltd Common CEQXF



GREY:CEQXF - Post by User

Post by EstevanOutsideron Nov 10, 2018 3:11pm
67 Views
Post# 28955430

NGTL pipeline deliveries down 1 bcf/d from 11/10/2017

NGTL pipeline deliveries down 1 bcf/d from 11/10/2017I went over some values today after a friend of mine informed me that there is a compressor issue on the Nova Transmission system that he thinks is blocking in about 450,000 mcf/d of gas on Segment 4.  

This is some data I found on the NGTL website daily log for flows:

[MMCF]
Nov 10: 6600 (2018) vs 7636 (2017) vs 6269 (2016)
Nov 09: 6715 (2018) vs 7653 (2017) vs 6238 (2016) 
Nov 01: 6398 (2018) vs 6585 (2017) vs 6791 (2016)
Oct 01: 6646 (2018) vs 6803 (2017) vs 7037 (2016) 
Oct 31: 6486 (2018) vs 6525 (2017) vs 6831 (2016)

There is a whopping 1 bcf/d difference between today and last year.  I went through most gas producer Q3s and Q2 and production cutbacks was pretty much a staple aside from guys like Encana and Tourmaline who have diversified away from AECO.

I am hoping that this is a sign of production cutbacks rather then maintenance.

Exprohibition, do you have any feedback on this?  
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