RE:Keephills 1From the Q3 SEDAR filing, page 11. See
Q3 filing
Keephills Unit 1
On March 5, 2013, an outage occurred at Unit 1 of our Keephills facility due to a stator winding failure found in the generator. Upon completion of the initial repair work, further condition testing and analysis identified greater winding degradation requiring a full rewind of the generator stator. In response to the event, we gave notice of a High Impact Low Probability event and claimed force majeure relief under the PPA. In the event of a force majeure, we are entitled to continue to receive our PPA capacity payment and are protected under the terms of the PPA from having to pay availability penalties. As a result, we do not expect the outage to have
a material financial impact on the Corporation. The Unit was returned to service on Oct. 6, 2013. Arbitration on the matter began during the quarter.